Saturday, March 28, 2020

Today in History

Today in History
Three Mile Island
1979

The Three Mile Island accident was a partial meltdown of reactor number 2 of Three Mile Island Nuclear Generating Station (TMI-2) in Dauphin County, Pennsylvania, near Harrisburg, and subsequent radiation leak that occurred on March 28, 1979. It was the most significant accident in U.S. commercial nuclear power plant history.[2] On the seven-point International Nuclear Event Scale, the incident was rated a five as an "accident with wider consequences".[3][4]

The accident began with failures in the non-nuclear secondary system, followed by a stuck-open pilot-operated relief valve in the primary system, which allowed large amounts of nuclear reactor coolant to escape. The mechanical failures were compounded by the initial failure of plant operators to recognize the situation as a loss-of-coolant accident due to inadequate training and human factors, such as human-computer interaction design oversights relating to ambiguous control room indicators in the power plant's user interface.

In particular, a hidden indicator light led to an operator manually overriding the automatic emergency cooling system of the reactor because the operator mistakenly believed that there was too much coolant water present in the reactor and causing the steam pressure release.[5]

The accident crystallized anti-nuclear safety concerns among activists and the general public, and resulted in new regulations for the nuclear industry. It has been cited as a contributor to the decline of a new reactor construction program, a slowdown that was already underway in the 1970s.[6] The partial meltdown resulted in the release of radioactive gases and radioactive iodine into the environment.

Anti-nuclear movement activists expressed worries about regional health effects from the accident.[7] However, epidemiological studies analyzing the rate of cancer in and around the area since the accident determined there was a small statistically non-significant increase in the rate and thus no causal connection linking the accident with these cancers has been substantiated.[8][9][10][11][12][13]

Cleanup started in August 1979, and officially ended in December 1993, with a total cleanup cost of about $1 billion.[14]


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